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beach fails to fix halifax-1 flow rates still, page-6

  1. 8 Posts.
    The Halifax-1 well had a peak gas flow rate of 4.2 MMscf/d, however, due to a faulty temperature gauge, this rate resulted in the maximum recommended temperature for the wellhead being exceeded. The faulty temperature gauge was discovered prior to shut-in of the well due to rain, at which point the well was flowing at 3.5 MMscf/d. After the well was re-opened, it flowed briefly at 4.5 MMscf/d, with the well immediately choked back to 2.0 MMscf/d to maintain temperatures within desired operating conditions, at which level it remained for the majority of March. The well is now flowing an unconstrained 1.7MMscf/d and currently flowing back stimulation fluid.


    Well flowing 3.5MMscf/d before shut in
    After shut in flowed 4.5MMscf/d before being choked back to 2MMscf/d

    The well is now flowing 1.7MMscf/d unconstrained.

    The combination of a decreased rate and a removal of the choke implies that the pressures have declined.
 
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