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sp valuation & analysis, page-16

  1. Ya
    6,809 Posts.
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    PW

    Without knowing the pipe dia, might take a stab at this.

    My thoughts on 2 possibilities:

    1) It could either b 7" casing joints that might b shipped to the OP for a C&S, or

    2) A really remote possibility that they may opt to sidetrack, which means set the plug, cut a window higher up in the 12.25" casing & then build up angle. The later Ops, needs different bit & hardware. (Once again, we dont know the pipe dia, so my guestimate).

    As per their 30th Dec update (page 3 & 4 seismics) shows that the well appears to have been drilled very close to a fault & the 45m thk highly porous SST reservoir (frm 421-466m as per the gamma ray logs) abuts against this fault, so any HC's (if present initially) have either seeped out thro' this fault &/or r accumulated towards the closure/dome & that the JV drilled the well in the wrong location.

    Which could mean that they may opt to ST & redrill thro' the top, where the HC's mayb accumulated. Just a theory at this point in time.

    Once again these r my views & could b mere waffle by the time they release their update on Tues (4th Jan).
 
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