88E 16.7% 0.3¢ 88 energy limited

Ann: Project Icewine Operations Update, page-3

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    4 September 2017
    88 Energy Limited
    Project Icewine Operations Update
    88 Energy Limited (“88 Energy”, “the Company”, “Operator”) (ASX, AIM: 88E) is pleased to provide
    an update on Project Icewine, located onshore North Slope of Alaska.
    Highlights
    • Flow testing on Icewine#2 re-commenced 31st August 10:26 (AK time) post ~7 week shut-in
    • Currently flowing back naturally on 4/64 choke at ~70 barrels per day frac fluid
    • Minor hydrocarbon indications via formation of gas hydrates within the choke manifold
    • Pressure data analysis indicates limited connection to the reservoir prior to last 24 hours
    Icewine#2 Operations Update
    The Icewine#2 well was shut-in on 10th July to allow for imbibition and pressure build up to occur within
    the HRZ shale. Flow testing re-commenced on 31st August at 10:26 (AK time), and is ongoing. Results
    since flow testing recommenced are summarised below.
    The Icewine#2 well is located on the North Slope of Alaska (ADL 392301). 88 Energy Ltd (via its
    wholly owned subsidiary, Accumulate Energy Alaska, Inc) has a 77.55% working interest in the well.
    The well was stimulated in two stages over a gross 128 foot vertical interval in the HRZ shale
    formation, from 10,957-11,085ft TVD, using a slickwater treatment comprising 27,837 barrels of fluid
    and 1,034,838 pounds of proppant.
    The well was initially flowed back on a 6/64 inch choke and was reduced to a 4/64 inch choke after 26
    hours to maintain pressure. Approximately 370 barrels of frac fluid had been recovered as at 1730 on
    3rd September (AK time) at an average rate of 100 barrels per day. Hydrocarbon indications have
    been minor and are associated only with the formation of gas hydrates in the choke manifold. Methanol
    injection has been initiated to prevent the surface manifold equipment from freezing thereby ensuring
    free flow of produced fluids through the choke.
    Wellhead pressure built to ~3,500psi during shut-in and has dropped to 1,130psi since flowback
    commenced. Initial analysis of the pressure data from both the build-up and flowback indicates limited
    connection to the reservoir prior to the last 24 hours. At 0550 on the 2nd September (AK time) a small
    pressure build-up was observed, potentially indicating the first contribution to pressure from the
    reservoir itself. This is the first time that this has occurred since flow testing was initiated, including
    the previous testing period prior to shut-in. To date the cumulative amount of stimulation fluid produced
    from both testing periods is 4,802 barrels, 17.25% of fluids injected.
    The current flowback procedure is early stage and the significance of an implied pressure contribution
    from the reservoir and formation of gas hydrates cannot yet be determined.
 
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