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Since last report on Thursday October 11th, drill pipe...

  1. 160 Posts.
    Since last report on Thursday October 11th, drill pipe conveyed
    logging has been conducted. Drillpipe conveyed logs rather than
    wireline logs have been run to TD due the angle of the well and
    hole condition.
    Preliminary interpretation of these logs indicates:
    a) The Anderson Sands have some zones with potential oil
    saturations. The commercial significance of those zones
    will require formation testing to evaluate. Testing of the
    Anderson zones would follow operations to evaluate the
    deeper Nullara Formation. A joint venture decision on
    testing of the Anderson awaits availability of the test
    program and any relevant information to be derived from
    testing the Nullara Fm.
    b) The top of Nullara Formation has been interpreted at
    2722m MD. Below 2732m MD, the log quality is severely
    degraded by interpreted large scale vugular porosity such
    that quantitative interpretation is not possible.
    In addition to earlier reported drilling fluid (mud) losses into the
    Nullara section there have been continued losses while
    conditioning the well for logging and preparing to case the hole.
    Because of the losses and subsequent lack of mud and cuttings
    returns, there is no indication of fluid content in the Nullara
    porous section. As of 0600 today the wellbore is now properly
    stabilised and the forward plan is to run 178mm (7”) casing prior
    to testing the Nullara Formation.
    While the loss of mud to the Nullara Fm has created operational
    difficulties that have now been overcome, we are encouraged by
    the presence of both porosity and significant permeability in the
    Nullara reef section. Development of vugular porosity in this
    section is a well recognised play, having previously been the
    target of exploration in the Basin, and we note that it is host to oil
    production at Blina some 100km to the SE.
    The planned test of the Nullara Formation will determine fluid
    type and flow characteristics of the reservoir. The Stokes Bay
    intersection of the Nullara Fm is 80m up dip of the Pt Torment 1
    intersection which did not have the vugular porosity developed,
    but nevertheless tested gas at low rates.
 
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