5GN 1.67% 15.3¢ 5g networks limited.

stokesbay

  1. 8,138 Posts.
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    Since last report on Thursday October 11th, Stokes Bay-1 ha
    been deepened from 1841mMD to present TD of 2755mMD.
    Stokes Bay-1 was drilled to a depth of 2589 metres at 1930
    hours on 15 October 2007, having intersected the origina
    primary objective; the Carboniferous aged Anderson Formation.
    Subsequently, ARC Energy Limited (Operator) proposed to the
    EP 104/R1 Joint Venture that the well be deepened from 2589
    metres to approximately 2800 metres to evaluate the Uppe
    Devonian aged Nullara carbonates. This recommendation wa
    based on the favourable information gained from the recen
    Valentine wellbore and recognition that the Nullara carbonate
    reef level produces oil at Blina, and had strong shows in the
    nearby Point Torment 1 well. Parties electing to participate in the
    deepening operation and their respective equity levels in this par
    of the Stokes Bay-1 well (below 2589mMD) are:
    • ARC Energy Limited – 69.25% (Operator)
    • Emerald Oil & Gas NL - 12.75%
    • Pancontinental Oil & Gas NL - 10.0%
 
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Last
15.3¢
Change
0.003(1.67%)
Mkt cap ! $47.66M
Open High Low Value Volume
15.0¢ 15.3¢ 15.0¢ $182.7K 1.218M

Buyers (Bids)

No. Vol. Price($)
11 1949454 15.0¢
 

Sellers (Offers)

Price($) Vol. No.
15.5¢ 1986841 27
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